Lost a lot of "friends" over this photo of Notre-Dame next to a tattoo I got maybe 6 months before the bitch burnt down. Hallelujah!
Thursday, December 10, 2020
Friday, November 13, 2020
Miata Dump
Some photos sent to me from a FullLock MacPark event earlier this year when the miatas front sub frame and frame rails were still straight and it didn't look like a rolling piece of shit.
Another couple photos from the last event of 2020, Fulllock at OMC. Obviously this is after my wreck with the 350z I posted about earlier. Looks terrible...the sub frame is tweaked and the hood latch is off by about 2 inches which is why it's hood-less, but its good enough and still rips.
Slowly working on the new miata... I'll update when its worth while.
Sunday, October 18, 2020
Bunny Hop Your Local Tweaker To Flat
The skate park tweakers under Kellogg normally clear out by 7:00am or so, but this guy kept the party going well into the afternoon having discussions with China, finding a good spot to light up, and dancing/rapping (?). Oblivious to anything going on around him, I decided to snag a photo of me bunny hopping over him to flat when he decided to set up shop in the bowl to fight the wind. Sadly some "hero" mom called the cops and he got hauled away before he came down and I could thank him for the hours of entertainment.
Thursday, October 8, 2020
Monday, September 21, 2020
Integra Distributor Leaks
Took the integra out a couple of a weeks ago and noticed a bunch oil all over the firewall. Changed the distributor o-ring and still had issues. The cap had oil in it so I changed the distributor shaft seal. Took a while to arrive since I had to order one, but it came in a few days ago and I got it installed over the weekend. Problem solved and way cheaper than buying a new distributor that I only use part of since I have the C.O.P. conversion.
Saturday, September 12, 2020
Thirty for Thirty
I made it to level 3 this year and decided to film thirty clips in 3 hours on the morning of my birthday. Otis and I got to the park around 7:30am just in time to hangout with all the crackheads. After they cleared out I set the camera on my camera bag and got started. Here's a short video of the results. Nothing too crazy since I'm terrified of knocking myself out when riding solo, but whatever; 30 clips is a lot of fucking work.
Here's to another 30 years on two wheels!
Thursday, August 27, 2020
Good Enough
Still need to yank the core support over to get the hood to latch, but it's good enough for now and it doesn't look THAT bad I suppose. Headlights even work! Now two of my three running cars are hoodless...time to get the integras painted and FINALLY installed 4-5 years later.
New front LCAs, driverside UCA and long bolt, tie rod ends, ball joints, tie rods, and steering rack up replaced up front. Feels decent even with my eyeball alignment. Hoping Alec can get it sorted out here in a few weeks before the Mac Park event mid-September. I also put the godspeed rear UCAs on while I was at it since this thing needs a full alignment anyway and I want to see how minimal rear camber feels. I'm ready to rip this thing again. Shouts out to Alec for making me put this back together.
The new miatas pre mandrel bent DOM tubing spec miata cage parts came in, waiting on the straight DOM tubing to get here and I'll be starting that soon.Updates whenever it's worth it.
Monday, August 24, 2020
Fast & Loose
Tuesday, July 28, 2020
welp, here we go.
Sunday, July 19, 2020
Another Wreck...
Damage report:
The driverside headlight, fender, LCA, endlink, and turn signal are fucked. Core support is shifted a little; I think I can bend the frame back though. The OEM impact bracket or whatever is crunched (I'll take them off)Hood isn't bad, I think the brackets deformed a little..I should be able to get that back to "normal" to where its barely noticeable once the frame is straightened. The passenger fender buckled also. I think my outer tie rod ends are okay? I'll know once I pull the rack. Got the headlight motor to work too.
Plans are to get new driver and passenger LCA's, a new steering rack (been long over due), inner tie rods, maybe outers?, fabricate a bash bar, new turn signal (IDK if I want OEM or the intake style), stitch the bumper, and end-links. Hopefully that's all it takes to get it feeling normal again. I might wind up having to replace parts later on that I haven't noticed, like the lower coil=over bushing, but we'll see.
Kind of sucks, but whatever; it happens. Drifting is still tight as fuck.